{"id":22997,"date":"2022-09-12T09:00:00","date_gmt":"2022-09-12T08:00:00","guid":{"rendered":"https:\/\/www.engineernewsnetwork.com\/blog\/?p=22997"},"modified":"2022-09-10T16:39:18","modified_gmt":"2022-09-10T15:39:18","slug":"rebuilding-a-13-5mw-hydro-generator","status":"publish","type":"post","link":"https:\/\/www.engineernewsnetwork.com\/blog\/rebuilding-a-13-5mw-hydro-generator\/","title":{"rendered":"Rebuilding a 13.5MW hydro generator"},"content":{"rendered":"\n<p>Hydropower generation sites across the UK have been delivering clean and renewable energy for decades. To ensure continued reliable operation, major components, such as generators need to be overhauled to prevent unexpected downtime. When the generator at the Dinas power station developed a fault, they awarded the project to refurbish the generator to <strong><a href=\"http:\/\/www.sulzer.com\" target=\"_blank\" rel=\"noreferrer noopener\">Sulzer<\/a>.<\/strong><\/p>\n\n\n\n<p>Opened in 1964 and located near Aberystwyth, the Dinas hydropower station is part of the largest hydro-electric scheme in England and Wales. After 56 years in operation, the generator at the facility had reached the point where a major overhaul was required.<\/p>\n\n\n\n<p><strong>Project assessment<\/strong><\/p>\n\n\n\n<p>Operated by Statkraft, the generator is a 15 MVA, 12.1kV, 13.5 \u00a0 MW (18,100hp) unit that is driven by a Francis turbine. The original stator was built in two halves that were transported to the site and assembled during the 1960s. Since then, the generator has reliably delivered power to the local grid for over half a century. However, eventually some of the winding insulation started to break down and an earth fault was detected, which led to the decision to rewind and rebuild the generator.<\/p>\n\n\n\n<p>Engineers from Statkraft disassembled the stator and discovered damage to the core as well as a coil failure. These issues set in motion a tender process and Sulzer was awarded the project.<\/p>\n\n\n<div class=\"wp-block-image\">\n<figure class=\"aligncenter size-full\"><a href=\"https:\/\/www.engineernewsnetwork.com\/blog\/wp-content\/uploads\/2022\/09\/SulzerDMA365_Pic2_PR7181_51748-scaled.jpg\"><img loading=\"lazy\" decoding=\"async\" width=\"2560\" height=\"1830\" src=\"https:\/\/www.engineernewsnetwork.com\/blog\/wp-content\/uploads\/2022\/09\/SulzerDMA365_Pic2_PR7181_51748-scaled.jpg\" alt=\"\" class=\"wp-image-22999\" srcset=\"https:\/\/www.engineernewsnetwork.com\/blog\/wp-content\/uploads\/2022\/09\/SulzerDMA365_Pic2_PR7181_51748-scaled.jpg 2560w, https:\/\/www.engineernewsnetwork.com\/blog\/wp-content\/uploads\/2022\/09\/SulzerDMA365_Pic2_PR7181_51748-300x214.jpg 300w\" sizes=\"auto, (max-width: 2560px) 100vw, 2560px\" \/><\/a><figcaption>Sulzer rebuilt the core concentric to within 0.15 mm and circular from top to bottom to within 0.05mm<\/figcaption><\/figure>\n<\/div>\n\n\n<p><strong>Challenging circumstances<\/strong><\/p>\n\n\n\n<p>During initial site visits, Sulzer confirmed the project scope and assessed the building as well as the equipment that was available at the facility to help complete the repair. The first task was to install a new three-phase distribution board and improve the electrical system so that it could safely support the equipment that would be required during the project. The installation of a fire alarm, spill kits and first aid equipment was routine, but there was also a need for heaters and dehumidifiers because the atmosphere inside the turbine building was around 95% humidity.<\/p>\n\n\n\n<p>One of the first challenges was the rotor, which contained asbestos from the original manufacturing process. Statkraft wanted to retain the copper rotor poles and Sulzer was able to provide a solution to recover them safely.<\/p>\n\n\n\n<p>Having established that the stator core would need to be replaced as well, Sulzer was essentially left with the generator frame as the starting point. The new core was built up using sectioned laminations to create a complete assembly without any gaps. In fact, Sulzer rebuilt the core concentric to within six-thousandths of an inch (0.15mm) and circular from top to bottom to within two-thousandths of an inch (0.05mm); a considerable improvement on the original.<\/p>\n\n\n<div class=\"wp-block-image\">\n<figure class=\"aligncenter size-full\"><a href=\"https:\/\/www.engineernewsnetwork.com\/blog\/wp-content\/uploads\/2022\/09\/SulzerDMA365_Pic3_PR7181_51754-scaled.jpg\"><img loading=\"lazy\" decoding=\"async\" width=\"2560\" height=\"1831\" src=\"https:\/\/www.engineernewsnetwork.com\/blog\/wp-content\/uploads\/2022\/09\/SulzerDMA365_Pic3_PR7181_51754-scaled.jpg\" alt=\"\" class=\"wp-image-23000\" srcset=\"https:\/\/www.engineernewsnetwork.com\/blog\/wp-content\/uploads\/2022\/09\/SulzerDMA365_Pic3_PR7181_51754-scaled.jpg 2560w, https:\/\/www.engineernewsnetwork.com\/blog\/wp-content\/uploads\/2022\/09\/SulzerDMA365_Pic3_PR7181_51754-300x215.jpg 300w\" sizes=\"auto, (max-width: 2560px) 100vw, 2560px\" \/><\/a><figcaption>The hydrogen brazing stations (centre) saved six days on the rebuild time<\/figcaption><\/figure>\n<\/div>\n\n\n<p><strong>Expanding expertise<\/strong><\/p>\n\n\n\n<p>Two teams of winders were assigned to this project to work round-the-clock and ensure the generator repair was completed within the customer\u2019s expectations. The teams consisted of three experienced winders and two younger apprentices who are learning the skills required for these projects. In this case, the teams were drawn from Sulzer\u2019s network of service centres, including Falkirk, Ipswich and Middlesbrough.<\/p>\n\n\n\n<p>Adrian Larmour, UK Sales Manager at Sulzer explains: \u201cSulzer is being proactive in training and developing the engineering skills of the next generation. There are many different designs of stator and larger hydro-electric equipment needs to be rewound onsite so our younger team members can learn a lot from a project like this one.\u201d<\/p>\n\n\n\n<p>Once the windings had been installed, the team built a tent structure over the stator and installed a series of heaters to bring the ambient temperature up to 180\u00b0C, which was then maintained for three days to cure the windings.<\/p>\n\n\n\n<p>In all, 227 new coils were designed, manufactured and tested in Sulzer\u2019s Birmingham Service Center. Of these, 216 were destined for the stator, with two spares for the build team and five spares for the customer. The remaining four coils were tested to destruction according to the specifications for hydro-electric applications and subjected to some of the most arduous test routines.<\/p>\n\n\n<div class=\"wp-block-image\">\n<figure class=\"aligncenter size-large\"><a href=\"https:\/\/www.engineernewsnetwork.com\/blog\/wp-content\/uploads\/2022\/09\/SulzerDMA365_Pic4_JPG_PR7181_51761-scaled.jpg\"><img loading=\"lazy\" decoding=\"async\" width=\"1024\" height=\"682\" src=\"https:\/\/www.engineernewsnetwork.com\/blog\/wp-content\/uploads\/2022\/09\/SulzerDMA365_Pic4_JPG_PR7181_51761-1024x682.jpg\" alt=\"\" class=\"wp-image-23001\" srcset=\"https:\/\/www.engineernewsnetwork.com\/blog\/wp-content\/uploads\/2022\/09\/SulzerDMA365_Pic4_JPG_PR7181_51761-1024x682.jpg 1024w, https:\/\/www.engineernewsnetwork.com\/blog\/wp-content\/uploads\/2022\/09\/SulzerDMA365_Pic4_JPG_PR7181_51761-300x200.jpg 300w, https:\/\/www.engineernewsnetwork.com\/blog\/wp-content\/uploads\/2022\/09\/SulzerDMA365_Pic4_JPG_PR7181_51761-768x511.jpg 768w, https:\/\/www.engineernewsnetwork.com\/blog\/wp-content\/uploads\/2022\/09\/SulzerDMA365_Pic4_JPG_PR7181_51761-1536x1023.jpg 1536w, https:\/\/www.engineernewsnetwork.com\/blog\/wp-content\/uploads\/2022\/09\/SulzerDMA365_Pic4_JPG_PR7181_51761-2048x1364.jpg 2048w, https:\/\/www.engineernewsnetwork.com\/blog\/wp-content\/uploads\/2022\/09\/SulzerDMA365_Pic4_JPG_PR7181_51761-310x205.jpg 310w\" sizes=\"auto, (max-width: 1024px) 100vw, 1024px\" \/><\/a><figcaption>Spare coils were manufactured for Statkraft as part of the project<\/figcaption><\/figure>\n<\/div>\n\n\n<p><strong>Advanced repair technology<\/strong><\/p>\n\n\n\n<p>Sulzer has invested in the latest in hydrogen brazing technology, which not only saved six days on the rebuild time, but is also less demanding in terms of health and safety requirements. Traditional oxy-acetylene brazing uses lower temperatures, requires a set of gas bottles for each brazing station and the process produces fumes that need to be extracted away from the working area. In contrast, hydrogen brazing uses increased temperatures and produces water as the only by-product.<\/p>\n\n\n\n<p>The process uses a hydrogen generator, which converts water to hydrogen gas that is supplied to a number of brazing stations. The higher heat concentration speeds up the brazing process and means that there is no need to reinstate the insulation after it has been completed, saving time for the project. In this case, three brazing stations were set up in the center of the stator, allowing the coil connection process to be completed much quicker.<\/p>\n\n\n\n<p>Adrian concludes: \u201cThe investment in the hydrogen brazing equipment is an example of our ongoing commitment to further strengthen our service offering. For our customers, it means we can optimize the project times and keep downtime to a minimum.\u201d<\/p>\n\n\n\n<p>A process of continuous communication with Statkraft\u2019s local engineers as well as advanced repair methods have ensured that the overall project was completed to the highest standards. The extensive refurbishment of the generator will deliver continued reliable operation for decades to come.<\/p>\n","protected":false},"excerpt":{"rendered":"<p>Hydropower generation sites across the UK have been delivering clean and renewable energy for decades. To ensure continued reliable operation, major components, such as generators need to be overhauled to prevent unexpected downtime. When the generator at the Dinas power station developed a fault, they awarded the project to refurbish the generator to Sulzer. Opened &hellip;<\/p>\n","protected":false},"author":1,"featured_media":22998,"comment_status":"closed","ping_status":"closed","sticky":false,"template":"","format":"standard","meta":{"footnotes":""},"categories":[107],"tags":[10773,10775,108],"class_list":["post-22997","post","type-post","status-publish","format-standard","has-post-thumbnail","","category-power","tag-hydro-generator","tag-statkraft","tag-sulzer"],"yoast_head":"<!-- This site is optimized with the Yoast SEO plugin v27.2 - https:\/\/yoast.com\/product\/yoast-seo-wordpress\/ -->\n<title>Rebuilding a 13.5MW hydro generator - Engineer News Network<\/title>\n<meta name=\"robots\" content=\"index, follow, max-snippet:-1, max-image-preview:large, max-video-preview:-1\" \/>\n<link rel=\"canonical\" href=\"https:\/\/www.engineernewsnetwork.com\/blog\/rebuilding-a-13-5mw-hydro-generator\/\" \/>\n<meta property=\"og:locale\" content=\"en_GB\" \/>\n<meta property=\"og:type\" content=\"article\" \/>\n<meta property=\"og:title\" content=\"Rebuilding a 13.5MW hydro generator - Engineer News Network\" \/>\n<meta property=\"og:description\" content=\"Hydropower generation sites across the UK have been delivering clean and renewable energy for decades. To ensure continued reliable operation, major components, such as generators need to be overhauled to prevent unexpected downtime. When the generator at the Dinas power station developed a fault, they awarded the project to refurbish the generator to Sulzer. 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